Ok the motors not moving in reverse makes sense now since they are not homed, and No I havent messed around with the steps per mm, in the firmware right? I could see how that would throw off accurate movement but shouldn't the motor still move just the wrong distance? Like if I jog the motor 100 units or connect it to the extrusion driver it should move just not say the exact 100 units right? Or would this stop the motors from doing anything?
↧