Hey guys :)
I am currently building a 3D Printer with much inspiration from that: [www.thingiverse.com]
However after a lot of troubleshooting I got most off it working, expect the y-motor is making a highpitch noise when it stands still.
I am running 5 Watterott TMC2130 on a MKS GEN 1.4 with Hardware SPI.
M122 Output:
I´ve tried everything: switching motors, connections, stepper. So I guess no Hardware problem?
I think, I setup something up wrong in the MarlinFW. So I tried different configurations but cant get this damn motor quit. :?
I have no idea what I could try anymore. I know there are some strange things in the M122 Output at Y, but I dont know what I have to tune to get it right.
Any Ideas?
I am currently building a 3D Printer with much inspiration from that: [www.thingiverse.com]
However after a lot of troubleshooting I got most off it working, expect the y-motor is making a highpitch noise when it stands still.
I am running 5 Watterott TMC2130 on a MKS GEN 1.4 with Hardware SPI.
M122 Output:
Recv: X Y Z Z2 E0 Recv: Enabled false false false false false Recv: Set current 850 900 600 850 700 Recv: RMS current 826 887 581 826 673 Recv: MAX current 1165 1251 819 1165 949 Recv: Run current 26/31 28/31 18/31 26/31 21/31 Recv: Hold current 13/31 14/31 9/31 13/31 10/31 Recv: CS actual 13/31 14/31 9/31 13/31 10/31 Recv: PWM scale 132 98 101 163 53 Recv: vsense 1=.18 1=.18 1=.18 1=.18 1=.18 Recv: stealthChop true true true true true Recv: msteps 16 16 16 16 16 Recv: tstep 1048575 1048575 1048575 1048575 1048575 Recv: pwm Recv: threshold 79 4294967295 658 658 263 Recv: [mm/s] 100.08 0.00 3.00 3.00 30.06 Recv: OT prewarn false false false false false Recv: OT prewarn has Recv: been triggered true true true true true Recv: off time 5 5 5 5 5 Recv: blank time 24 24 24 24 24 Recv: hysteresis Recv: -end 2 2 2 2 2 Recv: -start 3 3 3 3 3 Recv: Stallguard thrs 4 0 0 0 0 Recv: DRVSTATUS X Y Z Z2 E0 Recv: stallguard X Recv: sg_result 0 0 0 0 0 Recv: fsactive Recv: stst X X X X X Recv: olb Recv: ola Recv: s2gb Recv: s2ga Recv: otpw Recv: ot Recv: Driver registers: X = 0x80:0D:00:00 Recv: Y = 0x81:0E:00:00 Recv: Z = 0x80:09:00:00 Recv: Z2 = 0x80:0D:00:00 Recv: E0 = 0x80:0A:00:00
I´ve tried everything: switching motors, connections, stepper. So I guess no Hardware problem?
I think, I setup something up wrong in the MarlinFW. So I tried different configurations but cant get this damn motor quit. :?
I have no idea what I could try anymore. I know there are some strange things in the M122 Output at Y, but I dont know what I have to tune to get it right.
Any Ideas?